Preparation of activated carbons doped with iron oxide for removing phenol within pilot-scaled three-phase fluidized bed
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Title Preparation of activated carbons doped with iron oxide for removing phenol within pilot-scaled three-phase fluidized bed
Creator Sukhum Chaeysiri
Contributor Tawatchai Charinpanitkul
Publisher Chulalongkorn University
Publication Year 2552
Keyword Phenol, Carbon, Activated, Fluidized reactors, Ferric oxide
Abstract Activated carbons doped with iron oxide were prepared for decomposition of aqueous phenol in three-phase fluidized bed reactor. The gas, liquid and solid phases in the reactor were ozone, aqueous phenol and Fe/activated carbon, respectively. Two types of activated carbon (AC-US and AC-TH) with average pore diameter of 2.3 and 1.7 nm and specific surface area of 1,060 and 1,154 m2/g, relatively were to use in this work. Based on laboratory-scaled investigation AC-TH was selected used in large-scaled experiments. 5 wt.% Fe on activated carbons were prepared by two techniques, namely wet impregnation (IMA) and incipient wetness impregnation (IMB). After impregnated and calcined at 500°C under nitrogen gas, 5%CAT-TH-A-500 could be prepared from IMA and 5%CAT-TH-B-500 form IMB. With 10 wt.% of Fe precursor, 10%CAT-TH-B-500 was prepared. With 5 wt.% of Fe precursor and calcined at 200°C under ambient air, 5%CAT-TH-B-200 was prepared. All activated carbons combined with ozone could provide detectable phenol and TOC removal efficiency. The sequence of phenol removal efficiency in a period of 60 minutes was as follows: 5%CAT-TH-B-500 + O3 (99%) = 5%CAT-TH-A-500 + O3 (99%) > AC-TH + O3 (98%) > 10%CAT-TH-B-500 + O3 (97%) > 5%CAT-TH-B-200 + O3 (90%) > only O3 (67%). The sequence of TOC removal efficiency at 360 min was as follows: AC-TH + O3 (92%) > 5%CAT-TH-B-200 + O3 (81%) > 5%CAT-TH-A-500 + O3 (71%) = 10%CAT-TH-B-500 + O3 (71%) > 5%CAT-TH-B-500 + O3 (69%) > only O3 (52%). However, AC-TH and 5%CAT-TH-B-200 could provide the hightest efficiency for TOC removal. In pilot-scaled three-phase fluidized bed reactor, the experiments were carried out using 200 L of 20 ppm aqueous phenol with AC-TH + O3 and 5%CAT-TH-B-200 + O3. It was found that 5%CAT-TH-B-200 exhibited with good stability even after repeated use in three consecutive runs (1,080 minutes) in pilot-scaled system. Usable lifetime of 18 hours could be verified from experiments using re-used activated carbon
URL Website cuir.car.chula.ac.th
Chulalongkorn University

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